Abstract
In order to ensure the safety and comfort of passengers and staff, an underground railway requires an extensive ventilation and cooling system. One mechanism for underground railway ventilation is the movement of air induced by trains, termed the 'piston effect'. This study investigated the effect of altering the blockage ratio of an underground train upon the ventilating air flows driven by a train. First a computational model was developed and validated with experimental data from literature. This model was scaled to represent an operational underground railway with high blockage ratio and the blockage ratio varied to evaluate the effects upon ventilation. The results of this study show that ventilating air flows can be increased significantly during periods of constant train motion and acceleration, by factors of 1.4 and 2 respectively, but that the train drag will increase at the same rate. During deceleration negligible increases in ventilation flows are found but drag increases by a factor of 4.
| Original language | English |
|---|---|
| Pages (from-to) | 195-206 |
| Number of pages | 12 |
| Journal | Journal of Wind Engineering and Industrial Aerodynamics |
| Volume | 146 |
| Early online date | 1 Oct 2015 |
| DOIs | |
| Publication status | Published - 1 Nov 2015 |
Funding
The authors would like to thank Guy Brammer Associates and the EPSRC in supporting this work through an EPSRC Industrial CASE Award (grant number 200593789 ).
Keywords
- aerodynamics
- computational fluid dynamics
- high blockage ratio
- underground railways
- ventilation
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